10/26/2021 |
The (10/26/2021, C-129) application [57940] was assigned to this incident. |
10/26/2021 |
Additional Details provided by the operator: The leak was caused by external corrosion in the flow line with the hole in the top 1/3 of the flowline. The hole was 0.030" .The leak was downstream of the separator and no hydrocarbons were found when excavated. Gas loss determination was 67 |
10/26/2021 |
Corrective actions provided by the operator: Line repaired and continue to inspect locations. |
10/26/2021 |
Primary Equipment identified by the operator (Flow Line - Production, with additional details: Epic Energy excavated and found the natural gas leak that had been reported on the EPIC Energy, Lybrook South #13 well location yesterday, October 14th. The leak was caused by external corrosion in the flow line with the hole in the top 1/3 of the flowline. The hole was 0.030" .The leak was downstream of the separator and no hydrocarbons were found when excavated. Gas loss determination was 67) |
10/26/2021 |
Steps taken to prevent waste provided by the operator: Continue to inspect wells. |
10/26/2021 |
New incident created by the operator, upon the submission of a venting of natural gas report. |
10/07/2021 |
The venting of natural gas discovered by the operator. |