OCD Permitting

NAPP2129956585 2021 MINOR I VENT @ 30-043-20838

General Incident Information

[30-043-20838] LYBROOK SOUTH #013

[372834] EPIC ENERGY, L.L.C.
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

Aztec
Minor
Indian
Sandoval (43)

C-19-23N-06W      0 FNL      0 FEL
36.2159271,-107.512223 NAD83


Notes

Industry Rep















Contact Details


Event Dates

10/07/2021
03:00 PM

10/07/2021
07:00 PM
10/22/2021

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [57940] 10/26/2021 10/26/2021
Notification [57940] 10/26/2021 10/26/2021

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 10/26/2021 68 2 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Corrosion Flow Line - Production Natural Gas Vented 67 0 67 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
10/26/2021 The (10/26/2021, C-129) application [57940] was assigned to this incident.
10/26/2021 Additional Details provided by the operator: The leak was caused by external corrosion in the flow line with the hole in the top 1/3 of the flowline. The hole was 0.030" .The leak was downstream of the separator and no hydrocarbons were found when excavated. Gas loss determination was 67
10/26/2021 Corrective actions provided by the operator: Line repaired and continue to inspect locations.
10/26/2021 Primary Equipment identified by the operator (Flow Line - Production, with additional details: Epic Energy excavated and found the natural gas leak that had been reported on the EPIC Energy, Lybrook South #13 well location yesterday, October 14th. The leak was caused by external corrosion in the flow line with the hole in the top 1/3 of the flowline. The hole was 0.030" .The leak was downstream of the separator and no hydrocarbons were found when excavated. Gas loss determination was 67)
10/26/2021 Steps taken to prevent waste provided by the operator: Continue to inspect wells.
10/26/2021 New incident created by the operator, upon the submission of a venting of natural gas report.
10/07/2021 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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