OCD Permitting

NAPP2203952374 2021 MINOR I FLAR @ FAPP2129154362

General Incident Information


[fAPP2129154362] Cotton Draw 3 CS
[4323] CHEVRON U S A INC
Closure Approved
Flare
Hobbs
Minor

Lea (25)

H-03-25S-32E      0 FNL      0 FEL
32.1533333,-103.6609722 NAD83


Notes

Industry Rep














Contact Details


Event Dates

12/31/2021
09:05 PM

12/31/2021
10:15 PM
02/08/2022

02/08/2022

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 02/08/2022 72 4 10 7 0

Incidents Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Gas Compressor Station Natural Gas Flared 296 0 296 Mcf

Incident Events

Date Detail
02/08/2022 The (02/08/2022, C-129) application [79785] was assigned to this incident.
02/08/2022 Corrective actions provided by the operator: Corrective measures focused on reducing gas production as quickly and safely as possible to minimize the duration and volume of gas flared.
02/08/2022 Steps taken to prevent waste provided by the operator: All of the facilities and emissions control devices at this site are operating as designed and, where applicable, are authorized. Chevron field personnel will execute practicable measures to minimize emissions.
02/08/2022 New incident created by the operator, upon the submission of a flaring of natural gas report.
12/31/2021 The flaring of natural gas discovered by the operator.

Orders No Orders Found

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