OCD Permitting

NAPP2035749293 29-6-70 PIPELINE @ 0

General Incident Information
29-6-70 PIPELINE

[fAPP2123052765] HARVEST FOUR CORNERS GATHER SYSTEM
[373888] Harvest Four Corners, LLC
Incident Closure Approved
Natural Gas Release

Aztec
Major
Private
Rio Arriba (39)

M-29-29N-06W      0 FNL      0 FEL
36.692056,-107.490981 NAD83


Notes

Industry Rep





Referred to Environmental Inspector









Contact Details

Monica Smith
Environmental Specialist

Event Dates

12/21/2020

1/5/2021

03/22/2021  

Incident Dates

Type Action Received Denied Approved
Remediation Closure Report 06/13/2022
Initial C-141 Report 12/28/2020 12/28/2020
Notification [12951] 12/22/2020 12/22/2020

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Pipeline (Any) [OBSOLETE] Natural Gas (Methane) 6055 0 6055 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        
Cause of Release OR Additional Details provided for materials released:
Affected Wells are SH 29-6 #70B; 70, 63A, 213, 63C, 5M and 212. Line has a large split of approximately 6.5" X 1/2".

Incident Events

Date Detail
06/13/2022 Closure Report Approved, Release Resolved.
06/13/2022 The (06/13/2022, C-141) application [13166] was accepted by OCD. The operator was emailed with details of this event.
06/13/2022 An application [13166] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
12/28/2020 The (06/13/2022, C-141) application [13166] was assigned to this incident.
12/22/2020 The (12/22/2020, NOR) application [12951] was accepted by OCD. The operator was emailed with details of this event.
12/22/2020 An application [12951] was submitted to OCD for review. It was submitted, indicating that it was an: [NOR] Notification of a release The operator was emailed confirmation of this event.
12/22/2020 The (12/22/2020, NOR) application [12951] was assigned to this incident.
12/22/2020 Additional Details provided by the operator: Affected Wells are SH 29-6 #70B; 70, 63A, 213, 63C, 5M and 212. Line has a large split of approximately 6.5" X 1/2".
12/22/2020 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: True.
  • All free liquids and recoverable materials have been removed and managed appropriately: True.
12/22/2020 New incident created by the operator, upon the submission of notification of release.
12/21/2020 C-141 received on 12/28/2020 for release on 12/21/2020. The cause of the release was reported as “Natural gas release, no liquids. It was caused by a split of approximately 6.5"x0.5" in the gas line.”
12/21/2020 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (3) an unauthorized release of gases exceeding 500 MCF.

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

         


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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