OCD Permitting

NAPP2102540540 LATERAL M-11 @ 0

General Incident Information
LATERAL M-11

[fAPP2123052765] HARVEST FOUR CORNERS GATHER SYSTEM
[373888] Harvest Four Corners, LLC
Incident Closure Approved
Natural Gas Release

Aztec
Major
Federal
Rio Arriba (39)

L-26-29N-04W      0 FNL      0 FEL
36.693056,-107.231389 NAD83


Notes

Industry Rep





Referred to Environmental Inspector









Contact Details

Kijun Hong

Event Dates

01/18/2021

2/2/2021

08/09/2022  

Incident Dates

Type Action Received Denied Approved
Remediation Closure Report 07/02/2021 05/11/2022
Remediation Plan 07/02/2021 05/11/2022
Site Characterization 07/02/2021 05/11/2022
Initial C-141 Report 01/29/2021

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Pipeline (Any) [OBSOLETE] Natural Gas (Methane) 3427 0 3427 Mcf
Equipment Failure Other (Specify) Produced Water 20 20 0 GAL
Equipment Failure Other (Specify) Condensate 10 10 0 GAL
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
05/11/2022 Closure Report Approved. Release Resolved.
05/11/2022 The (05/11/2022, C-141) application [34864] was accepted by OCD. The operator was emailed with details of this event.
07/02/2021 The (05/11/2022, C-141) application [34864] was assigned to this incident.
04/29/2021 Reviewed Operator Request for Extension. Operator failed to notify the USFS of release, release location was in an arch site. Remediation must cease and Arch survey must be completed etc. Granted Extension to submit closure report to July 2, 2021.
02/05/2021 The (02/05/2021, C-141) application [16192] was accepted by OCD. The operator was emailed with details of this event.
02/05/2021 An application [16192] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
01/29/2021 The (02/05/2021, C-141) application [16192] was assigned to this incident.
01/25/2021 The (01/25/2021, NOR) application [15520] was accepted by OCD. The operator was emailed with details of this event.
01/25/2021 An application [15520] was submitted to OCD for review. It was submitted, indicating that it was an: [NOR] Notification of a release The operator was emailed confirmation of this event.
01/25/2021 The (01/25/2021, NOR) application [15520] was assigned to this incident.
01/25/2021 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: True.
  • All free liquids and recoverable materials have been removed and managed appropriately: True.
01/25/2021 New incident created by the operator, upon the submission of notification of release.
01/18/2021 C-141 received on 1/29/2021 for release on 1/18/2021. The cause of the release was reported as “caused by a crack of approximately 4"x0.25" in the 4" gas line”
01/18/2021 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (2) an unauthorized release of a volume that:
                (b) may with reasonable probability reach a watercourse;
        (3) an unauthorized release of gases exceeding 500 MCF;
        (4) a release of a volume that may with reasonable probability be detrimental to fresh water.

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

         


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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