OCD Permitting

NAPP2108343786 MOORE 3A @ 0

General Incident Information
MOORE 3A

[fAPP2123052765] HARVEST FOUR CORNERS GATHER SYSTEM
[373888] Harvest Four Corners, LLC
Initial C-141 Approved, Pending submission of Site Characterization / Remediation Plan OR Remediation Closure Report from the operator
Natural Gas Release

Aztec
Minor
Private
San Juan (45)

J-05-31N-09W      0 FNL      0 FEL
36.924166,-107.80251 NAD83


Notes

Industry Rep





Referred to Environmental Inspector









Contact Details

Kijun Hong

Event Dates

03/15/2021

3/30/2021

06/14/2021  

Incident Dates

Type Action Received Denied Approved
Initial C-141 Report 03/30/2021 03/30/2021
Notification [21826] 03/24/2021 03/24/2021

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Pipeline (Any) [OBSOLETE] Natural Gas (Methane) 72 0 72 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/26/2021 The (04/26/2021, C-141) application [22383] was accepted by OCD. The operator was emailed with details of this event.
04/26/2021 An application [22383] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
03/30/2021 The (04/26/2021, C-141) application [22383] was assigned to this incident.
03/24/2021 The (03/24/2021, NOR) application [21826] was assigned to this incident.
03/24/2021 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: True.
  • All free liquids and recoverable materials have been removed and managed appropriately: True.
03/24/2021 New incident created by the operator, upon the submission of notification of release.
03/15/2021 C-141 received on 3/30/2021 for release on 3/15/2021. The cause of the release was reported as “A gasket leak was found on the meter run. The meter run was isolated, the leak was stopped, and the gasket was replaced. No liquids. Gas loss volume based on: estimated Port size .250”, estimated average pressure during the event 88 psi, estimated duration 783 minutes.”
03/15/2021 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

         


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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