| 06/10/2021 |
The (06/10/2021, C-129) application [31456] was assigned to this incident. |
| 06/10/2021 |
Additional Details provided by the operator: The Black Marlin pipeline is understand and cannot take the amount of gas the produced. The Max Allowable Operating Pressure cannot take the gas production and there is abundance of H2S gas that was not expected. |
| 06/10/2021 |
Corrective actions provided by the operator: The well has been choked back as of 6/10 and Tap Rock is making strides to get equipment out there for a goal of 100% gas capture. |
| 06/10/2021 |
Steps taken to prevent waste provided by the operator: Tap Rock Operating received flare volumes for this facility on 6/9/2021 and have reported this within 24 hrs of discovery. The well has been choked back as of 6/10 and Tap Rock is making strides to get equipment out there for a goal of 100% gas capture. |
| 06/10/2021 |
New incident created by the operator, upon the submission of a venting of natural gas report. |
| 05/25/2021 |
The venting of natural gas discovered by the operator. |