OCD Permitting

NAPP2127148672 2021 MINOR I FLAR @ 0

General Incident Information

[fAPP2126327768] Driver 14 FED COM CTB FL
[7377] EOG RESOURCES INC
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

N-14-23S-33E      0 FNL      0 FEL
32.3001152,-103.5436522 NAD83
Hobbs
State
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

09/27/2021
02:00 AM

09/27/2021
05:00 PM
10/12/2021

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [52452] 09/28/2021 09/28/2021
Notification [52452] 09/28/2021 09/28/2021

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 09/28/2021 100 0 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Pipeline (Any) Natural Gas Flared 59 0 59 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
09/28/2021 The (09/28/2021, C-129) application [52452] was assigned to this incident.
09/28/2021 Corrective actions provided by the operator: Corrective actions are not in our control and reliant on outside source(s)
09/28/2021 Steps taken to prevent waste provided by the operator: Monitored event and volumes in real time when applicable and confirmed proper flare operating settings
09/28/2021 New incident created by the operator, upon the submission of a flaring of natural gas report.
09/27/2021 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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