OCD Permitting

NAPP2130843222 2021 MINOR I FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

10/25/2021
12:00 AM

10/25/2021
11:59 PM
11/9/2021

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [60235] 11/04/2021 11/04/2021
Notification [60235] 11/04/2021 11/04/2021

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Gas Compressor Station Natural Gas Flared 159 0 159 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
11/04/2021 The (11/04/2021, C-129) application [60235] was assigned to this incident.
11/04/2021 Corrective actions provided by the operator: Repair, reset , restart
11/04/2021 Steps taken to prevent waste provided by the operator: Repaired
11/04/2021 New incident created by the operator, upon the submission of a flaring of natural gas report.
10/25/2021 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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