OCD Permitting

NAPP2135730208 2021 MINOR I FLAR @ 0

General Incident Information


[fAPP2132728185] STREETCAR 15 FED CTB
[7377] EOG RESOURCES INC
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

Hobbs
Minor
Federal
Lea (25)

O-15-25S-33E      0 FNL      0 FEL
32.123846,-103.559091 NAD83


Notes

Industry Rep















Contact Details


Event Dates

12/19/2021
12:00 AM

12/19/2021
11:59 PM
1/3/2022

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [68604] 12/23/2021 12/23/2021
Notification [68604] 12/23/2021 12/23/2021

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 12/23/2021 100 0 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Production Tank Natural Gas Flared 65 0 65 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
12/23/2021 The (12/23/2021, C-129) application [68604] was assigned to this incident.
12/23/2021 Corrective actions provided by the operator: Review downtime events and work to eliminate events causing downtime.
12/23/2021 Steps taken to prevent waste provided by the operator: Monitor in real time. When alarmed, identify and work to resolve source causing the downtime.
12/23/2021 New incident created by the operator, upon the submission of a flaring of natural gas report.
12/19/2021 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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