OCD Permitting

NAPP2201246679 2021 MINOR I FLAR @ 0

General Incident Information


[fAPP2129922540] Mesa 3H 16H
[260297] BTA OIL PRODUCERS, LLC
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

Hobbs
Minor
Federal
Lea (25)

M-01-26S-32E      0 FNL      0 FEL
32.06555,-103.63595 NAD83


Notes

Industry Rep















Contact Details


Event Dates

12/31/2021
12:00 AM

12/31/2021
11:59 PM
1/17/2022

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [71992] 01/12/2022 01/12/2022
Notification [71992] 01/12/2022 01/12/2022

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/12/2022 72 2 0 6 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Separator Natural Gas Flared 152 0 152 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/12/2022 The (01/12/2022, C-129) application [71992] was assigned to this incident.
01/12/2022 Corrective actions provided by the operator: Battery Redesign
01/12/2022 Primary Equipment identified by the operator (Separator)
01/12/2022 Steps taken to prevent waste provided by the operator: Battery Redesign
01/12/2022 New incident created by the operator, upon the submission of a flaring of natural gas report.
12/31/2021 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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