OCD Permitting

NAPP2201364627 SHUGART W 29 FED 3 WELLPAD @ 0

General Incident Information
SHUGART W 29 FED 3 WELLPAD


[6137] DEVON ENERGY PRODUCTION COMPANY, LP
Incident Closure Approved
Oil Release

Artesia
Minor
Federal
Eddy (15)

M-29-18S-31E      0 FNL      0 FEL
32.713916,-103.897022 NAD83


Notes

Industry Rep





Referred to Environmental Inspector









Contact Details

Wesley Mathews

Event Dates

12/31/2021

1/17/2022

03/31/2022  

Incident Dates

Type Action Received Denied Approved
Remediation Closure Report 06/30/2022 08/22/2022
Remediation Plan 06/30/2022
Site Characterization 06/30/2022
Initial C-141 Report 01/13/2022

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Other (Specify) Crude Oil 3 2 1 BBL
Other Other (Specify) Produced Water 4 1 3 BBL
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
08/22/2022 The (08/22/2022, C-141) application [121851] was accepted by OCD. The operator was emailed with details of this event.
08/22/2022 Closure Report Approved.
08/22/2022 An application [121851] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
06/30/2022 The (08/22/2022, C-141) application [121851] was assigned to this incident.
01/14/2022 The (01/14/2022, C-141) application [72354] was accepted by OCD. The operator was emailed with details of this event.
01/14/2022 An application [72354] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
01/13/2022 The (01/14/2022, C-141) application [72354] was assigned to this incident.
01/13/2022 The (01/13/2022, NOR) application [72352] was assigned to this incident.
01/13/2022 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: False.
  • All free liquids and recoverable materials have been removed and managed appropriately: True.
01/13/2022 New incident created by the operator, upon the submission of notification of release.
12/31/2021 C-141 received on 01/13/2022 for release on 12/31/2021. The cause of the release was reported as “Tubing caused fluid release. All fluid stayed on pad.”
12/31/2021 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

        Spill was not in containment.


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


Click to go back to top of page