OCD Permitting

NAPP2201364627 SHUGART W 29 FED 3 WELLPAD @ M-29-18S-31E 0N 0E

General Incident Information
SHUGART W 29 FED 3 WELLPAD


[6137] DEVON ENERGY PRODUCTION COMPANY, LP
Closure Not Approved
Oil Release
Artesia
Minor
Federal
Eddy (15)

M-29-18S-31E      0 FNL      0 FEL
32.713916,-103.897022 NAD83


Notes

Industry Rep





Referred to Environmental Inspector








Contact Details

Wesley Mathews

Event Dates

12/31/2021
01/13/2022
06/30/2022
06/30/2022

06/30/2022

03/31/2022

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incidents Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Other (Specify) Crude Oil 3 2 1 BBL
Other Other (Specify) Produced Water 4 1 3 BBL

Incident Events

Date Detail
06/30/2022 An application [121851] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
06/30/2022 The (06/30/2022, C-141) application [121851] was assigned to this incident.
01/14/2022 The (01/14/2022, C-141) application [72354] was accepted by OCD. The operator was emailed with details of this event.
01/14/2022 An application [72354] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
01/13/2022 The (01/14/2022, C-141) application [72354] was assigned to this incident.
01/13/2022 The (01/13/2022, NOR) application [72352] was assigned to this incident.
01/13/2022 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: False.
  • All free liquids and recoverable materials have been removed and managed appropriately: True.
01/13/2022 New incident created by the operator, upon the submission of notification of release.
12/31/2021 C-141 received on 01/13/2022 for release on 12/31/2021. The cause of the release was reported as “Tubing caused fluid release. All fluid stayed on pad.”
12/31/2021 Release discovered by the operator.

Orders No Orders Found

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