OCD Permitting

NAPP2210944637 2022 MINOR I VENT @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-18-18S-36E      0 FNL      0 FEL
32.74703,-103.39558 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

04/18/2022
09:45 AM

04/18/2022
03:00 PM
5/3/2022

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [99759] 04/19/2022 04/19/2022
Notification [99759] 04/19/2022 04/19/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 04/19/2022 75 2 1 1 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Corrosion Pipeline (Any) Natural Gas Vented 161 0 161 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/19/2022 The (04/19/2022, C-129) application [99759] was assigned to this incident.
04/19/2022 Corrective actions provided by the operator: line was shut in
04/19/2022 Primary Equipment identified by the operator (Pipeline (Any), with additional details: corrosion in pipeline causing line leak, line shut in for repair)
04/19/2022 Steps taken to prevent waste provided by the operator: line was shut in
04/19/2022 New incident created by the operator, upon the submission of a venting of natural gas report.
04/18/2022 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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