OCD Permitting

NAPP2211538701 2022 MAJOR I VENT @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-16-17S-34E      1 FNL      1 FEL
32.8409202,-103.5716494 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

04/23/2022
01:16 PM

04/23/2022
03:16 PM
5/9/2022

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [101184] 04/25/2022 04/25/2022
Notification [101184] 04/25/2022 04/25/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 04/25/2022 62 4 1 6 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Pipeline (Any) Natural Gas Vented 640 0 640 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/25/2022 The (04/25/2022, C-129) application [101184] was assigned to this incident.
04/25/2022 Corrective actions provided by the operator: verified leak on DCP BB line isolated line and blew down line segment
04/25/2022 Steps taken to prevent waste provided by the operator: verified leak on DCP BB line isolated line and blew down line segment
04/25/2022 New incident created by the operator, upon the submission of a venting of natural gas report.
04/23/2022 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


Click to go back to top of page