OCD Permitting

NAPP2214720646 2022 MAJOR I FLAR @ 0

General Incident Information

[fAPP2123047624] Bubbles
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

N-22-19S-30E      0 FNL      0 FEL
32.641274,-103.963861 NAD83
Artesia
Federal
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

05/26/2022
12:00 AM

05/26/2022
11:59 PM
6/10/2022

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [115490] 06/09/2022 06/09/2022
Notification [111479] 05/27/2022 05/27/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Gas Compressor Station Natural Gas Flared 852 0 852 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
06/09/2022 Corrective actions provided by the operator: No corrective actions taken at this site. Third party took corrective actions
06/09/2022 Steps taken to prevent waste provided by the operator: Verify pressure settings to flare.
06/09/2022 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
06/09/2022 The (06/09/2022, C-129A) application [115490] was assigned to this incident.
05/27/2022 The (05/27/2022, NOMVF) application [111479] was assigned to this incident.
05/27/2022 New incident created by the operator, upon the submission of a notification of venting or flaring.
05/26/2022 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


Click to go back to top of page