OCD Permitting

nAPP2215443701 SAN JUAN GAS PLANT

General Incident Information

[fGP00000000026] SAN JUAN GAS PLANT
[372171] HILCORP ENERGY COMPANY
Inactive
Incident Closure Approved
Natural Gas Release

D-14-29N-11W      0 FNL      0 FEL
36.731902,-107.968236 NAD83
Aztec
Private
San Juan (45)


Severity Indicators














Notes

Industry Rep
Referred to Environmental Inspector


Contact Details

Clara cordoza
Environmental Specialist

Event Dates

05/27/2022

6/13/2022

08/25/2022  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Remediation Closure Report 06/09/2022 06/23/2022
Initial C-141 Report 06/09/2022 06/09/2022
Notification 06/03/2022 06/03/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other (Specify) 0 0 0
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
06/23/2022 Closure Report Approved, Release Resolved.
06/23/2022 The (06/23/2022, C-141) application [115438] was accepted by OCD. The operator was emailed with details of this event.
06/23/2022 An application [115438] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
06/09/2022 The (06/23/2022, C-141) application [115438] was assigned to this incident.
06/03/2022 The (06/03/2022, NOR) application [113470] was assigned to this incident.
06/03/2022 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices:
  • All free liquids and recoverable materials have been removed and managed appropriately:
  • If all the actions described above have not been undertaken, explain why:
06/03/2022 New incident created by the operator, upon the submission of notification of release.
05/27/2022 C-141 received on 6/9/2022 for release on 05/27/2022. The cause of the release was reported as “Gasket failure on the demethanizer reboiler caused a release of natural gas liquids. No liquids reached the ground as it turned to vapor before anything accumulated”.
05/27/2022 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

         


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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