OCD Permitting

NAPP2218128453 2022 MAJOR I FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

06/29/2022
12:00 AM

06/29/2022
11:59 PM
7/14/2022

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [125270] 07/14/2022 07/14/2022
Notification [121740] 06/30/2022 06/30/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Power Failure Other (Specify) Natural Gas Flared 1883 0 1883 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
07/14/2022 Corrective actions provided by the operator: Repair, reset , restart
07/14/2022 Steps taken to prevent waste provided by the operator: Repaired
07/14/2022 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
07/14/2022 The (07/14/2022, C-129A) application [125270] was assigned to this incident.
06/30/2022 The (06/30/2022, NOMVF) application [121740] was assigned to this incident.
06/30/2022 New incident created by the operator, upon the submission of a notification of venting or flaring.
06/29/2022 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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