OCD Permitting

nAPP2221348013 KO LANTA 9 CTB 3

General Incident Information

[fAPP2130541074] KO LANTA 9 CTB 3
[6137] DEVON ENERGY PRODUCTION COMPANY, LP
Inactive
Incident Closure Approved
Oil Release

N-09-23S-31E      1000 FSL      2555 FWL
32.31448556,-103.7830889 NAD83
Artesia
Federal
Eddy (15)


Severity Indicators














Notes

Industry Rep
Referred to Environmental Inspector


Contact Details

Dale Woodall

Event Dates

08/01/2022

8/16/2022

10/16/2023  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Remediation Closure Report 03/08/2023 07/17/2023
Remediation Plan 03/08/2023 07/17/2023
Initial C-141 Report 08/15/2022 08/15/2022
Notification 08/01/2022 08/01/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Valve Crude Oil 70 20 50 BBL
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        
Cause of Release OR Additional Details provided for materials released:
6" CHECK VALVE ON THE SUCTION LINE OF THE LACT UNIT CRACKED AND STARTED TO LEAK ONTO THE GROUND. LEAK WAS NOT IN A LINED CONTAINMENT. LEAK DID NOT LEAVE LOCATION. LINE WAS ISOLATED TO STOP THE LEAK. 69.8 BBLS RELEASED. VACUUM TRUCKS DISPATCHED. RECOVERED VOLUMES NOT AVAILABLE AT THE TIME OF THIS REPORT.

Incident Events

Date Detail
07/17/2023 The (07/17/2023, C-141) application [194896] was accepted by OCD. The operator was emailed with details of this event.
07/17/2023 An application [194896] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
03/08/2023 The (07/17/2023, C-141) application [194896] was assigned to this incident.
08/15/2022 The (08/15/2022, C-141) application [134120] was accepted by OCD. The operator was emailed with details of this event.
08/15/2022 An application [134120] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
08/15/2022 The (08/15/2022, C-141) application [134120] was assigned to this incident.
08/01/2022 C-141 received on 8/15/2022 for release on 08/01/2022. The cause of the release was reported as “Valve on line developed leak”.
08/01/2022 C-141 received on 8/15/2022 for release on 08/01/2022. The cause of the release was reported as “Valve on line developed leak”.
08/01/2022 The (08/01/2022, NOR) application [130232] was assigned to this incident.
08/01/2022 Release discovered by the operator.
08/01/2022 Additional Details provided by the operator: 6" CHECK VALVE ON THE SUCTION LINE OF THE LACT UNIT CRACKED AND STARTED TO LEAK ONTO THE GROUND. LEAK WAS NOT IN A LINED CONTAINMENT. LEAK DID NOT LEAVE LOCATION. LINE WAS ISOLATED TO STOP THE LEAK. 69.8 BBLS RELEASED. VACUUM TRUCKS DISPATCHED. RECOVERED VOLUMES NOT AVAILABLE AT THE TIME OF THIS REPORT.
08/01/2022 Initial Response question & answers at the time of notification were as follows.
  • The source of the release has been stopped: True.
  • The impacted area has been secured to protect human health and the environment: True.
  • Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices: True.
  • All free liquids and recoverable materials have been removed and managed appropriately: False.
08/01/2022 New incident created by the operator, upon the submission of notification of release.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (1) an unauthorized release of a volume, excluding gases, of 25 barrels or more.

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

        6" CHECK VALVE ON THE SUCTION LINE OF THE LACT UNIT CRACKED AND STARTED TO LEAK ONTO THE GROUND. LEAK WAS NOT IN A LINED CONTAINMENT. LEAK DID NOT LEAVE LOCATION. LINE WAS ISOLATED TO STOP THE LEAK. 69.8 BBLS RELEASED. VACUUM TRUCKS DISPATCHED. RECOVERED VOLUMES NOT AVAILABLE AT THE TIME OF THIS REPORT.


No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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