| 09/30/2022 |
Corrective actions provided by the operator: Tap Rock was purging system after being shut in for an extended period of time. Due to this the system flared. Tap Rock also saw high line pressure from our midstream provider. The VRU malfunctioned and could not buck line pressure - causing excess gas to flare. Tap Rock is analyzing this location and the equipment on location to verify the facility can capture all excess gas after the system has been purged. If flaring continues Tap Rock will alter the facility by placing additional gas takeaway equipment. |
| 09/30/2022 |
Steps taken to prevent waste provided by the operator: Tap Rock was purging system after being shut in for an extended period of time. Due to this the system flared. Tap Rock also saw high line pressure from our midstream provider. The VRU malfunctioned and could not buck line pressure - causing excess gas to flare. Tap Rock is analyzing this location and the equipment on location to verify the facility can capture all excess gas after the system has been purged. If flaring continues Tap Rock will alter the facility by placing additional gas takeaway equipment. |
| 09/30/2022 |
Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report. |
| 09/29/2022 |
The (09/30/2022, C-129A) application [147576] was assigned to this incident. |
| 09/19/2022 |
The (09/19/2022, NOMVF) application [144465] was assigned to this incident. |
| 09/19/2022 |
New incident created by the operator, upon the submission of a notification of venting or flaring. |
| 09/18/2022 |
The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A. |