| 12/06/2022 |
Corrective actions provided by the operator: LP flare due to high gas line pressure causing the VRUs not to run which keeps the tank blower from being beneficial. MP flare extremely high due to diverting all LP flare down MP flare line for 4-5 hrs while the LP flare valve was pulled for repair, and due to smaller VRUs not bucking against line pressure. |
| 12/06/2022 |
Steps taken to prevent waste provided by the operator: LP flare due to high gas line pressure causing the VRUs not to run which keeps the tank blower from being beneficial. MP flare extremely high due to diverting all LP flare down MP flare line for 4-5 hrs while the LP flare valve was pulled for repair, and due to smaller VRUs not bucking against line pressure. |
| 12/06/2022 |
Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report. |
| 11/28/2022 |
The (12/06/2022, C-129A) application [161501] was assigned to this incident. |
| 11/28/2022 |
The (11/28/2022, NOMVF) application [161493] was assigned to this incident. |
| 11/28/2022 |
New incident created by the operator, upon the submission of a notification of venting or flaring. |
| 11/23/2022 |
The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A. |