OCD Permitting

NAPP2235354479 2022 MAJOR I FLAR @ 0

General Incident Information

[fAPP2126032949] TALCO CTB
[372043] TAP ROCK OPERATING, LLC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

C-16-26S-35E      308 FNL      1490 FWL
32.04972,-103.376993 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

12/18/2022
12:01 AM

12/18/2022
11:59 PM
1/2/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [168463] 01/08/2023 01/08/2023
Notification [168452] 12/19/2022 12/19/2022

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/08/2023 68 1 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Gas Compressor Station Natural Gas Flared 541 0 541 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/08/2023 Corrective actions provided by the operator: HP flare due to blowing down GL compressor 3 times. LP flare vol due to blower being off. MP flare due to removal of small VRUs 1,2. In the process of installing 200 hp VRU #1, new VRU should be in service today. Troubleshooting GL compressor, 2nd stage scrubber will not dump fluid correctly.
01/08/2023 Steps taken to prevent waste provided by the operator: HP flare due to blowing down GL compressor 3 times. LP flare vol due to blower being off. MP flare due to removal of small VRUs 1,2. In the process of installing 200 hp VRU #1, new VRU should be in service today. Troubleshooting GL compressor, 2nd stage scrubber will not dump fluid correctly.
01/08/2023 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
12/19/2022 The (01/08/2023, C-129A) application [168463] was assigned to this incident.
12/19/2022 The (12/19/2022, NOMVF) application [168452] was assigned to this incident.
12/19/2022 New incident created by the operator, upon the submission of a notification of venting or flaring.
12/18/2022 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


Click to go back to top of page