OCD Permitting

NAPP2307439128 2023 MINOR I FLAR @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

A-16-24S-32E      0 FNL      0 FEL
32.216800001,-103.674800001 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

03/14/2023
06:30 PM

03/14/2023
11:59 PM
3/29/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [197351] 03/15/2023 03/15/2023
Notification [197351] 03/15/2023 03/15/2023

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 03/15/2023 74 4 0 2 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Pipeline (Any) Natural Gas Flared 211 0 211 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
03/15/2023 The (03/15/2023, C-129) application [197351] was assigned to this incident.
03/15/2023 Corrective actions provided by the operator: line was isolated and flared off
03/15/2023 Primary Equipment identified by the operator (, with additional details: 69230)
03/15/2023 Steps taken to prevent waste provided by the operator: line was isolated and flared off
03/15/2023 New incident created by the operator, upon the submission of a flaring of natural gas report.
03/14/2023 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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