04/19/2023 |
Corrective actions provided by the operator: PSV was re-tested and passed on the next business day. Testing showed that the PSV should have relieved just below 650 psi. PSV was adjusted to be within 3% of the 650 psi set pressure |
04/19/2023 |
Primary Equipment identified by the operator (Valve) |
04/19/2023 |
Steps taken to prevent waste provided by the operator: Immediately upon discovery, Harvest personnel pinched back the block valve to get the PSV to reset, stopping the gas release |
04/19/2023 |
Incident updated by the operator, upon the submission of a amendment for venting of natural gas report. |
04/19/2023 |
The (04/19/2023, C-129A) application [208970] was assigned to this incident. |
04/15/2023 |
The (04/15/2023, NOMVF) application [208054] was assigned to this incident. |
04/15/2023 |
New incident created by the operator, upon the submission of a notification of venting or flaring. |
04/14/2023 |
The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A. |