OCD Permitting

NAPP2311027572 2023 MINOR I FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

04/09/2023
12:00 AM

04/09/2023
11:59 PM
4/24/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [209257] 04/20/2023 04/20/2023
Notification [209257] 04/20/2023 04/20/2023

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Production Tank Natural Gas Flared 87 0 87 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/20/2023 The (04/20/2023, C-129) application [209257] was assigned to this incident.
04/20/2023 Corrective actions provided by the operator: Repair, reset , restart
04/20/2023 Steps taken to prevent waste provided by the operator: Repaired
04/20/2023 New incident created by the operator, upon the submission of a flaring of natural gas report.
04/09/2023 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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