OCD Permitting

NAPP2314929387 2023 MAJOR I FLAR @ 0

General Incident Information

[fAB1902354255] REMUDA 100 BATTERY
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

E-25-23S-29E      0 FNL      0 FEL
32.27695,-103.94264 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

05/28/2023
12:00 AM

05/28/2023
11:59 PM
6/12/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [226368] 06/12/2023 06/12/2023
Notification [221397] 05/29/2023 05/29/2023

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Gas Compressor Station Natural Gas Flared 820 0 820 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
06/12/2023 Corrective actions provided by the operator: repair, reset, restart
06/12/2023 Steps taken to prevent waste provided by the operator: Repaired
06/12/2023 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
06/12/2023 The (06/12/2023, C-129A) application [226368] was assigned to this incident.
05/29/2023 The (05/29/2023, NOMVF) application [221397] was assigned to this incident.
05/29/2023 New incident created by the operator, upon the submission of a notification of venting or flaring.
05/28/2023 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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