OCD Permitting

NAPP2317137745 2023 MAJOR I FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

06/19/2023
12:00 AM

06/19/2023
11:59 PM
7/4/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [235685] 07/03/2023 07/03/2023
Notification [230632] 06/20/2023 06/20/2023

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Gas Compressor Station Natural Gas Flared 777 0 777 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
07/03/2023 Corrective actions provided by the operator: repair, reset, restart
07/03/2023 Steps taken to prevent waste provided by the operator: Repaired
07/03/2023 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
07/03/2023 The (07/03/2023, C-129A) application [235685] was assigned to this incident.
06/20/2023 The (06/20/2023, NOMVF) application [230632] was assigned to this incident.
06/20/2023 New incident created by the operator, upon the submission of a notification of venting or flaring.
06/19/2023 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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