07/24/2023 |
The (07/24/2023, C-129) application [243148] was assigned to this incident. |
07/24/2023 |
Additional Details provided by the operator: Leak identified in flyover week report. Notification made to Harvest 3rd party flyover contractor on 7/12/2023 at 12:21 pm, leak terminated, and line blocked in on 7/12/2023
Leak back calculated to 7/6/2023 10:34 AM. gas loss total 207.80 mcf |
07/24/2023 |
Corrective actions provided by the operator: Pipeline shut in and repairs to line made. |
07/24/2023 |
Primary Equipment identified by the operator (Pipeline (Any)) |
07/24/2023 |
Steps taken to prevent waste provided by the operator: Upon notification of leak, operations were routed to the area. Blocked in the pipeline and pressure tested to verify leak. The line remained isolated, and gas shut in. Until repairs could be made. |
07/24/2023 |
New incident created by the operator, upon the submission of a venting of natural gas report. |
07/12/2023 |
The venting of natural gas discovered by the operator. |