OCD Permitting

NAPP2329156029 2023 MINOR I FLAR @ 0

General Incident Information


[fAPP2127228708] MERCILESS 13 FED COM CTB
[7377] EOG RESOURCES INC
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

Hobbs
Minor

Lea (25)

B-13-25S-32E      0 FNL      0 FEL
32.135202,-103.62649 NAD83


Notes

Industry Rep















Contact Details


Event Dates

10/06/2023
12:00 AM

10/06/2023
11:59 PM
10/23/2023

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [277159] 10/18/2023 10/18/2023
Notification [277159] 10/18/2023 10/18/2023

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 10/18/2023 100 0 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Repair and Maintenance Producing Well Natural Gas Flared 108 0 108 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
10/18/2023 The (10/18/2023, C-129) application [277159] was assigned to this incident.
10/18/2023 Corrective actions provided by the operator: Implement a scheduled maintenance program to avoid failures
10/18/2023 Steps taken to prevent waste provided by the operator: Task is site specific but should have pre job planning meeting and look for ways to limit or avoid flaring
10/18/2023 New incident created by the operator, upon the submission of a flaring of natural gas report.
10/06/2023 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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