OCD Permitting

NAPP2330673895 2023 MINOR I VENT @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-20-17S-33E      0 FNL      0 FEL
32.82009,-103.68163 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

11/01/2023
03:30 PM

11/01/2023
05:00 PM
11/16/2023

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [282342] 11/02/2023 11/02/2023
Notification [282342] 11/02/2023 11/02/2023

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Pipeline (Any) Natural Gas Vented 62 0 62 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
11/02/2023 The (11/02/2023, C-129) application [282342] was assigned to this incident.
11/02/2023 Corrective actions provided by the operator: Repairs to pipeline in progress.
11/02/2023 Steps taken to prevent waste provided by the operator: Shut in line.
11/02/2023 New incident created by the operator, upon the submission of a venting of natural gas report.
11/01/2023 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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