OCD Permitting

NAPP2401066488 2024 MINOR AIA FLAR @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

A-19-22S-29E      0 FNL      0 FEL
32.37669419,-104.0212116 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

01/10/2024
10:49 AM

01/10/2024
04:37 PM
1/25/2024

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [302390] 01/10/2024 01/10/2024
Notification [302390] 01/10/2024 01/10/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/10/2024 95 2 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Pipeline (Any) Natural Gas Flared 449 0 449 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/10/2024 The (01/10/2024, C-129) application [302390] was assigned to this incident.
01/10/2024 Corrective actions provided by the operator: this is a different segment of the same line for this project related to event 89278 BF-Line 01092024 nAPP2401052203 sphera 3126475
01/10/2024 Steps taken to prevent waste provided by the operator: operations lowered the line pressure as much as possible before flaring the pipeline
01/10/2024 The flaring of natural gas discovered by the operator.
01/10/2024 New incident created by the operator, upon the submission of a flaring of natural gas report.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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