OCD Permitting

NAPP2405344523 2024 MINOR AIA FLAR @ 0

General Incident Information


[fAPP2129154362] Cotton Draw 3 CS
[4323] CHEVRON U S A INC
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

Hobbs
Minor

Lea (25)

H-03-25S-32E      0 FNL      0 FEL
32.153383,-103.660897 NAD83


Notes

Industry Rep















Contact Details


Event Dates

02/09/2024
11:49 PM

02/09/2024
11:59 PM
2/26/2024

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [316679] 02/22/2024 02/22/2024
Notification [316679] 02/22/2024 02/22/2024

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 02/22/2024 71 1 10 1 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Gas Compressor Station Natural Gas Flared 115 0 115 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
02/22/2024 The (02/22/2024, C-129) application [316679] was assigned to this incident.
02/22/2024 Corrective actions provided by the operator: Corrective measures focused on reducing gas production as quickly and safely as possible to minimize the duration and volume of gas flared.
02/22/2024 Steps taken to prevent waste provided by the operator: All the facilities and emissions control devices at this site are operating as designed and, where applicable, are authorized. Chevron field personnel executed practicable measures to minimize emissions.
02/22/2024 New incident created by the operator, upon the submission of a flaring of natural gas report.
02/09/2024 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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