OCD Permitting

NAPP2412126715 2024 MINOR AIA FLAR @ 0

General Incident Information

[fAPP2132728185] STREETCAR 15 FED CTB
[7377] EOG RESOURCES INC
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

O-15-25S-33E      0 FNL      0 FEL
32.123846,-103.559091 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

04/21/2024
03:00 AM

04/21/2024
01:00 PM
5/6/2024

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [338925] 04/30/2024 04/30/2024
Notification [338925] 04/30/2024 04/30/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 04/30/2024 26 2 7 3 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Pipeline (Any) Natural Gas Flared 158 0 158 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/30/2024 The (04/30/2024, C-129) application [338925] was assigned to this incident.
04/30/2024 Corrective actions provided by the operator: Corrective actions are not in our control and reliant on outside source(s)
04/30/2024 Steps taken to prevent waste provided by the operator: Monitored event and volumes in real time when applicable and confirmed proper flare operating settings
04/30/2024 New incident created by the operator, upon the submission of a flaring of natural gas report.
04/21/2024 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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