OCD Permitting

NAPP2427631008 2024 MAJOR AAA FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep
Referred to Environmental Inspector


Contact Details


Event Dates

10/02/2024
12:00 AM

10/02/2024
11:59 PM
10/17/2024

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [389993] 10/04/2024 10/04/2024
Notification [389119] 10/02/2024 10/02/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Other (Specify) Natural Gas Flared 3787 0 3787 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
10/04/2024 Corrective actions provided by the operator: Repair, reset, restart
10/04/2024 Steps taken to prevent waste provided by the operator: Repaired
10/04/2024 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
10/04/2024 The (10/04/2024, C-129A) application [389993] was assigned to this incident.
10/02/2024 The (10/02/2024, NOMVF) application [389119] was assigned to this incident.
10/02/2024 The event discovered by the operator; will be tracked as a Flare till submission of the required subsequent C-129A.
10/02/2024 New incident created by the operator, upon the submission of a notification of venting or flaring.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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