OCD Permitting

NAPP2510641957 2025 MINOR AIA FLAR @ 0

General Incident Information


[fAPP2131631171] HOLYFIELD 9 FED COM EAST/WEST CTB
[7377] EOG RESOURCES INC
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

Hobbs
Minor

Lea (25)

O-09-25S-34E      0 FNL      0 FEL
32.1406756,-103.479055 NAD83


Notes

Industry Rep















Contact Details


Event Dates

04/12/2025
12:00 AM

04/12/2025
10:00 PM
4/28/2025

 

Incident Dates

Type Action Received Denied Approved
Initial C-129 Report [452754] 04/16/2025 04/16/2025
Notification [452754] 04/16/2025 04/16/2025

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 04/16/2025 37 1 11 4 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Producing Well Natural Gas Flared 115 0 115 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/16/2025 The (04/16/2025, C-129) application [452754] was assigned to this incident.
04/16/2025 Corrective actions provided by the operator: Corrective actions are site specific but work to establish the best VRU run time
04/16/2025 Steps taken to prevent waste provided by the operator: Event is site specific but if present, work to get VRU back on line
04/16/2025 New incident created by the operator, upon the submission of a flaring of natural gas report.
04/12/2025 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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