05/13/2025 |
Primary Equipment identified by the operator (, with additional details: updated 05/13/2025 after investigation the gouge of the pipe was found to be smaller than originally estimated (est 2" gouge was actually 1.5") reducing the emissions to 4270mcf (see updated binder for calcs and pipeline damage). nlc) |
05/13/2025 |
Incident updated by the operator, upon the submission of a amendment for venting of natural gas report. |
05/13/2025 |
The (05/13/2025, C-129A) application [461434] was assigned to this incident. |
05/02/2025 |
The (05/02/2025, C-129) application [458169] was assigned to this incident. |
05/02/2025 |
Corrective actions provided by the operator: Ops isolated line and blew down pressure as well as shut in producers at the well head and the associated compressor station |
05/02/2025 |
Steps taken to prevent waste provided by the operator: Ops isolated line and blew down pressure as well as shut in producers at the well head and the associated compressor station |
05/02/2025 |
The venting of natural gas discovered by the operator. |
05/02/2025 |
New incident created by the operator, upon the submission of a venting of natural gas report. |