OCD Permitting

NAPP2512256806 2025 MAJOR AAA VENT @ 0

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-04-21S-32E      Lot: 1 0 FNL      0 FEL
32.510817,-103.673675 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

05/02/2025
10:13 AM

05/02/2025
01:30 PM
5/19/2025

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Amended C-129 Report [461434] 05/13/2025 05/13/2025
Initial C-129 Report [458169] 05/02/2025 05/02/2025
Notification [458169] 05/02/2025 05/02/2025

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 05/02/2025 76 3 0 1 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Pipeline (Any) Natural Gas Vented 4270 0 4270 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
05/13/2025 Primary Equipment identified by the operator (, with additional details: updated 05/13/2025 after investigation the gouge of the pipe was found to be smaller than originally estimated (est 2" gouge was actually 1.5") reducing the emissions to 4270mcf (see updated binder for calcs and pipeline damage). nlc)
05/13/2025 Incident updated by the operator, upon the submission of a amendment for venting of natural gas report.
05/13/2025 The (05/13/2025, C-129A) application [461434] was assigned to this incident.
05/02/2025 The (05/02/2025, C-129) application [458169] was assigned to this incident.
05/02/2025 Corrective actions provided by the operator: Ops isolated line and blew down pressure as well as shut in producers at the well head and the associated compressor station
05/02/2025 Steps taken to prevent waste provided by the operator: Ops isolated line and blew down pressure as well as shut in producers at the well head and the associated compressor station
05/02/2025 The venting of natural gas discovered by the operator.
05/02/2025 New incident created by the operator, upon the submission of a venting of natural gas report.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


Click to go back to top of page