OCD Permitting

NAPP2513229223 2025 MINOR AAA FLAR @ 0

General Incident Information

[fAPP2126039123] Nash Deep East TB
[5380] XTO ENERGY, INC
Inactive
Amended C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

M-18-23S-30E      0 FNL      0 FEL
32.300134,-103.914144 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

05/08/2025
12:00 AM

05/08/2025
11:59 PM
5/23/2025

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Amended C-129 Report [466192] 05/22/2025 05/22/2025
Initial C-129 Report [460777] 05/12/2025 05/12/2025
Notification [460777] 05/12/2025 05/12/2025

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Normal Operations Production Tank Natural Gas Flared 92 0 92 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
05/22/2025 Incident updated by the operator, upon the submission of a amendment for flaring of natural gas report.
05/22/2025 The (05/22/2025, C-129A) application [466192] was assigned to this incident.
05/12/2025 The (05/12/2025, C-129) application [460777] was assigned to this incident.
05/12/2025 Corrective actions provided by the operator: No corrective actions, normal ops
05/12/2025 Steps taken to prevent waste provided by the operator: Verify pressure settings to flare.
05/12/2025 New incident created by the operator, upon the submission of a flaring of natural gas report.
05/08/2025 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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