OCD Permitting

NAPP2535330656 2025 MINOR AIA FLAR @ FAPP2323430740

General Incident Information

[fAPP2323430740] SERPENTINE 35 FACILITY 1
[6137] DEVON ENERGY PRODUCTION COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Flare

L-35-22S-33E      1472 FSL      530 FWL
32.3450684,-103.5500574 NAD83
Hobbs
Lea (25)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

12/18/2025
12:00 AM

12/18/2025
10:22 AM
1/2/2026

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [536364] 12/19/2025 12/19/2025
Notification [536364] 12/19/2025 12/19/2025

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 12/19/2025 72 1 2 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
High Line Pressure Separator Natural Gas Flared 183 0 183 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
12/19/2025 The (12/19/2025, C-129) application [536364] was assigned to this incident.
12/19/2025 Corrective actions provided by the operator: Contacted 3rd party to determine when line pressure will decrease.
12/19/2025 Steps taken to prevent waste provided by the operator: Flaring stops when line pressure drops.
12/19/2025 New incident created by the operator, upon the submission of a flaring of natural gas report.
12/18/2025 The flaring of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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