OCD Permitting

nEEM0417546745 DCP SE NM GATHERING SYSTEM

General Incident Information

[fAPP2123031660] DCP SE NM Gathering System
[36785] DCP OPERATING COMPANY, LP
Inactive
Re-vegetation Report Approved, Restoration Complete
Natural Gas Release

F-18-17S-30E      0 FNL      0 FEL
32.836474,-104.013193 NAD83
Artesia
Federal
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

06/21/2004

7/6/2004

11/13/2018  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Re-vegetation Report 10/01/2024 10/01/2024
Remediation Closure Report Extension 08/15/2018 08/15/2018

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Gas Compressor Station [OBSOLETE] Natural Gas (Methane) 228 0 228 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
10/01/2024 Natural Gas Release Only
06/23/2004 Grayburg Booster Station. Grayburg #6 unit down on jacket water high temp. Grayburg #6 allowed to cool down and unit was restarted.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions
No initial response data was found for this incident.

No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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