OCD Permitting

NLWJ1010449406 2010 MAJOR A OS @ 30-025-38576

General Incident Information
[30-025-38576] LINAM AGI #001

[36785] DCP OPERATING COMPANY, LP
Active
Closure Not Approved, Pending submission of C-141 from the operator
Oil Release

K-30-18S-37E      1980 FSL      1980 FWL
32.7168083,-103.2928391 NAD83
Hobbs
State
Lea (25)


Severity Indicators














Notes

Industry Rep
Referred to Environmental Inspector


Contact Details


Event Dates

04/14/2010

4/29/2010

11/13/2018  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Remediation Closure Report Extension 08/15/2018 08/15/2018

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Flow Line - Production Natural Gas Liquids 25 0 25 BBL
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
04/14/2010 Leak was initially reported as -5 bbl, but excavation indicated reportable. Leak location J-4-2-7-4-ext Legal: E 8 19S 35E, areal dimension 7. 5'x100' (750 Sq Ft) 1RP# 2476

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (1) an unauthorized release of a volume, excluding gases, of 25 barrels or more.

Incident Corrective Actions
No initial response data was found for this incident.

No site characterization data was found for this incident.

No remediation plan data was found for this incident.

No active remediation deferral request was found for this incident.

No remediation closure report data was found for this incident.

No reclamation report data was found for this incident.

No re-vegetation report data was found for this incident.

Orders No Orders Found


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