02/15/2022 |
Incident cancelled by the operator, upon the submission of a [C-129] Cancel Venting and/or Flaring (C-129C) report. |
02/15/2022 |
The (02/15/2022, C-129C) application [81795] was assigned to this incident. |
01/13/2022 |
The (01/13/2022, C-129) application [70915] was assigned to this incident. |
01/13/2022 |
Additional Details provided by the operator: Wells previously shut-in due to nearby offset frac. While bringing wells back online, oxygen became present in production tanks. Flared gas until oxygen purged and we were able to reconnect gas to sales.
Flared 106 MCF total over Dec 30th and 31st; no liquid spilled |
01/13/2022 |
Corrective actions provided by the operator: Continue routine inspections and maintenance of facilities. |
01/13/2022 |
Primary Equipment identified by the operator (Production Tank, with additional details: O2 present in production tanks.) |
01/13/2022 |
Steps taken to prevent waste provided by the operator: Purged oxygen from tanks. |
01/13/2022 |
New incident created by the operator, upon the submission of a flaring of natural gas report. |
12/31/2021 |
The flaring of natural gas discovered by the operator. |