10/06/2023 |
The (10/06/2023, C-129) application [273421] was assigned to this incident. |
10/06/2023 |
Additional Details provided by the operator: Gas Flare Meter |
10/06/2023 |
Corrective actions provided by the operator: Oxy is unable to take any corrective actions to eliminate the cause and potential reoccurrence of a downstream third-party owned and operated gas plant’s issues, as this is downstream of Oxy’s custody transfer point and out of Oxy’s control to foresee, avoid, prevent from happening or reoccur. Enterprise will have issues which may reoccur from time to time and may trigger a spike in the gas line pressure, which in turn, directly impacts Oxy’s ability to send gas to them. When Enterprise has equipment issues or greatly struggles to handle the volume of gas being sent to them by Oxy, Enterprise then restricts Oxy’s ability to send gas, which then prompts Oxy to route all its stranded gas not pushed into the Enterprise’s gas pipeline, to flare. OXY makes every effort to control and minimize emissions as much as possible. The only actions that Oxy can take and handle that is within its control, is to continually communicate with Enterprise personnel, who own and operate the sales gas pipeline, when possible, during these types of circumstances. |
10/06/2023 |
Primary Equipment identified by the operator (Other (Specify), with additional details: Emergency Flare > Third Party Downstream Activity > Enterprise > Equipment Issues) |
10/06/2023 |
Steps taken to prevent waste provided by the operator: It is OXY's policy to route its stranded gas to a flare during an unforeseen and unavoidable emergency or malfunction, that is beyond Oxy's control to avoid, prevent or foresee, to minimize emissions as much as possible as part of the overall steps taken to limit duration and magnitude of flaring. The flare at this facility has a 98% combustion efficiency to lessen emissions as much as possible. In this case, Enterprise, third party owned and operated downstream pipeline operator, shut in their gas service several times within a 24-hr period to Oxy due to equipment issues on their end, which in turn caused high line pressure to occur, which then triggered brief intermittent flaring events to occur. This event could not have been foreseen, avoided or prevented from happening as each flaring instance which occurred, did so with no advance notice or warning. As soon as flaring was triggered, field personnel engaged in Oxy’s third party pipeline operation curtailment reactive stratagems and assisted with ensuring field area’s mitigation optimizers cut injection rates to wells in the field to reduce injection and sales gas across the area. This event is out of OXY's control, yet OXY made every effort to control and minimize emissions as much as possible. |
10/06/2023 |
New incident created by the operator, upon the submission of a flaring of natural gas report. |
09/21/2023 |
The flaring of natural gas discovered by the operator. |