OCD Permitting

nAPP2402330749 GRAYBURG BOOSTER STATION

General Incident Information

[fEEM0416235819] Grayburg Booster Station
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

F-18-17S-30E      0 FNL      0 FEL
32.836474,-104.013193 NAD83
Artesia
Federal
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

01/22/2024
02:30 PM

01/22/2024
03:15 PM
2/6/2024

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [306575] 01/23/2024 01/23/2024
Notification [306575] 01/23/2024 01/23/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/23/2024 68 3 0 2 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Gas Compressor Station Natural Gas Vented 109 0 109 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/23/2024 The (01/23/2024, C-129) application [306575] was assigned to this incident.
01/23/2024 Corrective actions provided by the operator: Restarted engines.
01/23/2024 Steps taken to prevent waste provided by the operator: Engines were restarted as quickly as possible.
01/23/2024 New incident created by the operator, upon the submission of a venting of natural gas report.
01/22/2024 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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