OCD Permitting

NAPP2407424683 2024 MINOR AIA VENT @ 0

General Incident Information

[fAB1526039763] Fitz Compressor Station
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-34-19S-29E      0 FNL      0 FEL
32.617100001,-104.059300001 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

03/13/2024
03:00 PM

03/13/2024
08:59 PM
3/28/2024

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [323122] 03/14/2024 03/14/2024
Notification [323122] 03/14/2024 03/14/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 03/14/2024 78 2 0 0 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Gas Compressor Station Natural Gas Vented 166 0 166 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
03/14/2024 The (03/14/2024, C-129) application [323122] was assigned to this incident.
03/14/2024 Corrective actions provided by the operator: None, started available compression as soon as possible.
03/14/2024 Steps taken to prevent waste provided by the operator: Started available compression and notified producers to shut in gas in order to bring field pressure below vent setpoint limit.
03/14/2024 New incident created by the operator, upon the submission of a venting of natural gas report.
03/13/2024 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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