OCD Permitting

nAPP2410756620 Willow Lake Gas Plant

General Incident Information

[fAPP2123159624] Crestwood New Mexico Pipeline
[330564] Crestwood New Mexico Pipeline LLC
Inactive
Re-vegetation Report Approved, Restoration Complete
Fire

A-29-24S-28E      0 FNL      0 FEL
32.194375,-104.103568 NAD83
Artesia
Private
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

04/15/2024

4/30/2024

09/09/2024  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Re-vegetation Report [353001] 06/11/2024 06/11/2024
Reclamation Report [353001] 06/11/2024 06/11/2024
Remediation Closure Report [353001] 06/11/2024 06/11/2024
Sampling Notice [352977] 06/11/2024 06/11/2024
Remediation Plan [353001] 06/11/2024 06/11/2024
Site Characterization [353001] 06/11/2024 06/11/2024
Initial C-141 Report [353001] 06/11/2024 06/11/2024
Notification [334144] 04/16/2024 04/16/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Fire Other (Specify) Natural Gas Flared 0 0 0 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        
Cause of Release OR Additional Details provided for materials released:
No release associated with this Incident.

Incident Events

Date Detail
06/11/2024 The (06/11/2024, C-141) application [353001] was accepted by OCD. The operator was emailed with details of this event.
06/11/2024 An application [353001] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
06/11/2024 The (06/11/2024, C-141) application [353001] was assigned to this incident.
06/11/2024 The (06/11/2024, C-141N) application [352977] was assigned to this incident.
04/16/2024 The (04/16/2024, NOR) application [334144] was assigned to this incident.
04/16/2024 New incident created by the operator, upon the submission of notification of release.
04/15/2024 Release discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (2) an unauthorized release of a volume that:
                (a) results in a fire or is the result of a fire.

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

         


Site Characterization

What is the shallowest depth to groundwater beneath the area affected by the release? Between 26 and 50 (ft.)   bgs
What method was used to determine the depth to ground water? NM OSE iWaters Database Search
Did this release impact groundwater or surface water? Yes No
Are the lateral extents of the release within 300 feet of a continuously flowing watercourse or any other significant watercourse? Between 1000 (ft.) and ½ (mi.)  
Are the lateral extents of the release within 200 feet of any lakebed, sinkhole, or playa lake (measured from the ordinary high-water mark)? Between 1000 (ft.) and ½ (mi.)  
Are the lateral extents of the release within 300 feet of an occupied permanent residence, school, hospital, institution, or church? Between ½ and 1 (mi.)  
Are the lateral extents of the release within 500 horizontal feet of a spring or a private domestic fresh water well used by less than five households for domestic or stock watering purposes? Between ½ and 1 (mi.)  
Are the lateral extents of the release within 1000 feet of any other fresh water well or spring? Between ½ and 1 (mi.)  
Are the lateral extents of the release within incorporated municipal boundaries or within a defined municipal fresh water well field? Between 1 and 5 (mi.)  
Are the lateral extents of the release within 300 feet of a wetland? Between 1000 (ft.) and ½ (mi.)  
Are the lateral extents of the release overlying a subsurface mine? Greater than 5 (mi.)  
Are the lateral extents of the release overlying an (non-karst) unstable area? Zero feet, overlying, or within area  
Categorize the risk of this well / site being in a karst geology? Medium  
Are the lateral extents of the release within a 100-year floodplain? Between ½ and 1 (mi.)  
Did the release impact areas not on an exploration, development, production, or storage site? Yes No

Remediation Plan

Have the lateral and vertical extents of contamination been fully delineated? Yes No
Was this release entirely contained within a lined containment area? Yes No
  Chloride *** (EPA 300.0 or SM4500 Cl B) 0   (mg/kg)
  TPH (GRO+DRO+MRO) (EPA SW-846 Method 8015M) 0   (mg/kg)
  GRO+DRO (EPA SW-846 Method 8015M) 0   (mg/kg)
  BTEX (EPA SW-846 Method 8021B or 8260B) 0   (mg/kg)
  Benzene (EPA SW-846 Method 8021B or 8260B) 0   (mg/kg)
On what estimated date will the remediation commence? 06/11/2024  
On what date will (or did) the final sampling occur? 06/11/2024  
On what date will (or was) the remediation complete(d) 06/11/2024  
What is the estimated surface area (in square feet) that will be reclaimed? 0   (sq ft)
What is the estimated volume (in cubic yards) that will be reclaimed? 0   (cu yds)
What is the estimated surface area (in square feet) that will be remediated? 0   (sq ft)
What is the estimated volume (in cubic yards) that will be remediated? 0   (cu yds)

This remediation will (or is expected to) utilize the following processes to remediate / reduce contaminants:

 

OTHER (Non-listed remedial process)?

None, insulation blanket fire. no liquids or gas released.


No active remediation deferral request was found for this incident.

Remediation Closure Report

Have the lateral and vertical extents of contamination been fully delineated? Yes No
Was this release entirely contained within a lined containment area? Yes No
All areas reasonably needed for production or subsequent drilling operations have been stabilized, returned to the sites existing grade, and have a soil cover that prevents ponding of water, minimizing dust and erosion? Yes No
What was the total surface area (in square feet) remediated? 0   (sq ft)
What was the total volume (cubic yards) remediated? 0   (cu yd)
All areas not reasonably needed for production or subsequent drilling operations have been reclaimed to contain a minimum of four feet of non-waste contain earthen material with concentrations less than 600 mg/kg chlorides, 100 mg/kg TPH, 50 mg/kg BTEX, and 10 mg/kg Benzene? Yes No
What was the total surface area (in square feet) reclaimed? 0   (sq ft)
What was the total volume (in cubic yards) reclaimed? 0   (cu yd)
OTHER (Non-listed remedial process)?

        N/A, insulation blanket fire. no liquids or gas released.


Reclamation Report

Have the lateral and vertical extents of contamination been fully delineated? Yes No
Was this release entirely contained within a lined containment area? Yes No
What was the total surface area (in square feet) reclaimed? 0.1   (sq ft)
What was the total volume (in cubic yards) reclaimed? 0.1   (cu yd)
Is the soil top layer complete and is it suitable material to establish vegetation? Yes No
On what estimated date was the reseeding to have commenced? 06/11/2024  
OTHER (Non-listed remedial process)?

        None, insulation blanket fire. no liquids or gas released.


No re-vegetation report data was found for this incident.

Orders No Orders Found


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