OCD Permitting

nAPP2421753870 ALDABRA 26 & 27 BATTERY

General Incident Information

[fAPP2129138007] ALDABRA 26 & 27 BATTERY
[6137] DEVON ENERGY PRODUCTION COMPANY, LP
Inactive
Liner Report Approved, Restoration Complete
Produced Water Release

P-26-23S-31E      350 FSL      455 FEL
32.2690001,-103.7409801 NAD83
Artesia
Private
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

08/04/2024

8/19/2024

01/28/2025  

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Remediation Closure Report [384251] 09/17/2024 10/30/2024
Liner Inspection Notice [376706] 08/22/2024 08/22/2024
Remediation Plan [384251] 09/17/2024 10/30/2024
Site Characterization [384251] 09/17/2024 10/30/2024
Initial C-141 Report [370209] 08/05/2024 08/05/2024
Notification [369711] 08/04/2024 08/04/2024

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

No Compositional Analysis Found


Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Equipment Failure Pump Produced Water 50 50 0 BBL
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        
Cause of Release OR Additional Details provided for materials released:
Swedge on transfer pump broke. 50 bbls produced water released into lined containment. 50 bbls recovered.

Incident Events

Date Detail
10/30/2024 App ID 384251: Liner inspection approved, release resolved.
10/30/2024 The (10/30/2024, C-141) application [384251] was accepted by OCD. The operator was emailed with details of this event.
10/30/2024 An application [384251] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
09/17/2024 The (10/30/2024, C-141) application [384251] was assigned to this incident.
08/22/2024 The (08/22/2024, C-141L) application [376706] was assigned to this incident.
08/05/2024 The (08/05/2024, C-141) application [370209] was accepted by OCD. The operator was emailed with details of this event.
08/05/2024 An application [370209] was submitted to OCD for review. It was submitted, indicating that it was an: [C-141] Application for administrative approval of a release notification and corrective action The operator was emailed confirmation of this event.
08/05/2024 The (08/05/2024, C-141) application [370209] was assigned to this incident.
08/04/2024 The (08/04/2024, NOR) application [369711] was assigned to this incident.
08/04/2024 Release discovered by the operator.
08/04/2024 New incident created by the operator, upon the submission of notification of release.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No
From paragraph A. Major release determine using:
        (1) an unauthorized release of a volume, excluding gases, of 25 barrels or more.

Incident Corrective Actions

Initial Response

The source of the release has been stopped.
The impacted area has been secured to protect human health and the environment.
Released materials have been contained via the use of berms or dikes, absorbent pads, or other containment devices.
All free liquids and recoverable materials have been removed and managed appropriately.
If all the actions described above have not been undertaken, explain why:

        Vacuum truck dispatched. 50 bbls recovered


Site Characterization

What is the shallowest depth to groundwater beneath the area affected by the release? Between 100 and 500 (ft.)   bgs
What method was used to determine the depth to ground water? NM OSE iWaters Database Search
Did this release impact groundwater or surface water? Yes No
Are the lateral extents of the release within 300 feet of a continuously flowing watercourse or any other significant watercourse? Greater than 5 (mi.)  
Are the lateral extents of the release within 200 feet of any lakebed, sinkhole, or playa lake (measured from the ordinary high-water mark)? Between 1 and 5 (mi.)  
Are the lateral extents of the release within 300 feet of an occupied permanent residence, school, hospital, institution, or church? Greater than 5 (mi.)  
Are the lateral extents of the release within 500 horizontal feet of a spring or a private domestic fresh water well used by less than five households for domestic or stock watering purposes? Between 1 and 5 (mi.)  
Are the lateral extents of the release within 1000 feet of any other fresh water well or spring? Between 1 and 5 (mi.)  
Are the lateral extents of the release within incorporated municipal boundaries or within a defined municipal fresh water well field? Greater than 5 (mi.)  
Are the lateral extents of the release within 300 feet of a wetland? Between 1 and 5 (mi.)  
Are the lateral extents of the release overlying a subsurface mine? Greater than 5 (mi.)  
Are the lateral extents of the release overlying an (non-karst) unstable area? Greater than 5 (mi.)  
Categorize the risk of this well / site being in a karst geology? Low  
Are the lateral extents of the release within a 100-year floodplain? Greater than 5 (mi.)  
Did the release impact areas not on an exploration, development, production, or storage site? Yes No

Remediation Plan

Have the lateral and vertical extents of contamination been fully delineated? Yes No
Was this release entirely contained within a lined containment area? Yes No
On what estimated date will the remediation commence?  
On what date will (or did) the final sampling occur?  
On what date will (or was) the remediation complete(d)  
What is the estimated surface area (in square feet) that will be remediated? 0   (sq ft)
What is the estimated volume (in cubic yards) that will be remediated? 0   (cu yds)
Is (or was) there affected material present needing to be removed
Is (or was) there a power wash of the lined containment area (to be) performed

OTHER (Non-listed remedial process)?


Release is indicated as entirely contained within a lined containment area. Deferral Requests are not expected; any received may not be granted for this incident.

Remediation Closure Report

Have the lateral and vertical extents of contamination been fully delineated? Yes No
Was this release entirely contained within a lined containment area? Yes No
What was the total surface area (in square feet) remediated? 0   (sq ft)
What was the total volume (cubic yards) remediated? 0   (cu yd)
OTHER (Non-listed remedial process)?

        see report


Release is indicated as entirely contained within a lined containment area. No Reclamation Report is expected or required for this incident at this time.

Release is indicated as entirely contained within a lined containment area. No Re-vegetation Report is expected or required for this incident at this time.

Orders No Orders Found


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