OCD Permitting

NAPP2502142722 2025 MINOR AIA VENT @ 0

General Incident Information

[fAB1526039763] Fitz Compressor Station
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-21-18S-26E      0 FNL      0 FEL
32.739200001,-104.387400001 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

01/20/2025
04:36 AM

01/20/2025
08:46 AM
2/4/2025

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [422810] 01/21/2025 01/21/2025
Notification [422810] 01/21/2025 01/21/2025

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/21/2025 78 2 0 1 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Gas Compressor Station Natural Gas Vented 224 0 224 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/21/2025 The (01/21/2025, C-129) application [422810] was assigned to this incident.
01/21/2025 Corrective actions provided by the operator: repaired regulator and started unit
01/21/2025 Steps taken to prevent waste provided by the operator: repaired regulator and started unit
01/21/2025 New incident created by the operator, upon the submission of a venting of natural gas report.
01/20/2025 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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