OCD Permitting

NAPP2602958498 2026 MINOR AIA VENT @ FEEM0416235819

General Incident Information

[fEEM0416235819] Grayburg Booster Station
[36785] DCP OPERATING COMPANY, LP
Inactive
Initial C-129 Accepted, Operator required to follow Monthly/Annual Waste Rule reporting requirements
Vent

A-18-17S-30E      0 FNL      0 FEL
32.8369,-104.0126 NAD83
Artesia
Eddy (15)


Severity Indicators














Notes

Industry Rep


Contact Details


Event Dates

01/28/2026
04:48 PM

01/28/2026
05:38 PM
2/12/2026

 

Incident Dates

19.15.29 NMAC - RELEASES

Type Action Received Denied Approved
Initial C-129 Report [548326] 01/29/2026 01/29/2026
Notification [548326] 01/29/2026 01/29/2026

19.15.30 NMAC - REMEDIATION

Type Action Received Denied Approved

Compositional Analysis of Vented and/or Flared Natural Gas

Date Methane
(CH4) %
Nitrogen
(N2) %
Hydrogen Suffide
(H2S) PPM
Carbon Dioxide
(CO2) %
Oxygen
(O2) %
Natural Gas Analysis 01/29/2026 67 3 1 1 0

Incident Materials

Cause Source Material Volume Units
Unk. Released Recovered Lost
Other Gas Compressor Station Natural Gas Vented 59 0 59 Mcf
 
The concentration of dissolved chloride in the produced water >10,000 mg/l:           Yes           No        

Incident Events

Date Detail
01/29/2026 The (01/29/2026, C-129) application [548326] was assigned to this incident.
01/29/2026 Corrective actions provided by the operator: Restarted units.
01/29/2026 Steps taken to prevent waste provided by the operator: Restarted units
01/29/2026 New incident created by the operator, upon the submission of a venting of natural gas report.
01/28/2026 The venting of natural gas discovered by the operator.

Incident Severity
Major release as defined by 19.15.29.7(A) NMAC?
Yes No

Incident Corrective Actions






Orders No Orders Found


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